Environment & Safety
Safety
We manage the safety of our workers through programs, systems, and standards, with our Safety, Health, Environment and Quality (SHEQ) Policy providing overarching guidance. There are many aspects of the management system that contribute to a safe work environment, a few examples include:
- Risk assessments help identify issues and determine the appropriate controls; the corrective action process verifies that incidents and near misses are reported, tracked, investigated and shared with colleagues; and emergency preparedness and planning prepare us to respond to serious incidents.
- We have developed 12 corporate safety standards to help protect our workers from our most common hazards. Some standards guide our general safety practices, such as our job hazard analysis and our job task observation, and other standards deal with specific hazardous situations (similar to other companies’ life saving rules): such as fall protection, confined space entry, rigging and hoisting, and control of hazardous energy (also referred to as lockout/tagout).
- Routine audits are conducted to monitor compliance with regulations and our own requirements. These and other aspects of the management system are routinely examined to verify that they continue to be effective at keeping our workers safe.
2020 | |
---|---|
McArthur River | 0.6 |
Key Lake | 1.0 |
Radiation Protection
Radiation risks are effectively managed at McArthur River and Key Lake. Each operation has a formal radiation protection program and dedicated personnel who ensure that doses to workers are as low as reasonably achievable. The programs require that radiation protection is considered in the physical design of all facilities and operating procedures. They also provide for systematic monitoring of radiation in work areas and track exposures of individual workers using a combination of monitoring devices and health testing. Radiation exposures at McArthur River and Key Lake are far below below the regulated limits.
Environmental Protection
At Cameco, protection of the environment is one of our highest corporate priorities during all stages of our activities, from exploration through development, operations, decommissioning, and reclamation.
We monitor our performance by tracking corporate and site-specific key performance indicators, conducting environmental monitoring programs, and regularly auditing our adherence to the requirements of these programs We use the information from all of our programs to help us to identify opportunities to improve.
Environmental management system
We have a ISO 14001-certified environmental management system used across our operating sites, which is supported by a corporate Environmental Management Program that outlines the operating requirements sites must meet. Our environmental management system encourages and promotes continuous adaptation of our practices based on new information and technologies.
Environmental risk assessments
We complete environmental risk assessments to systematically identify, quantify, and to characterize the potential risks to the environment, workers, and the public. We use our environmental risk assessments to inform our decisions and actions. Additionally, we complete an iterative process, where required, to verify that our proposed measures to protect the environment and the public are effective. We review or update the assessments every five years, incorporating results from our environmental monitoring programs and other scientific advances.
Environmental performance reports
For our Saskatchewan operations, every five years we also compare monitoring data collected during the reporting period against predictions contained in approved environmental risk assessments or environmental assessments. By reviewing the data from the performance reports and conducting risks assessments, we are able to demonstrate that human health and the environment in the vicinity of our Saskatchewan operations remains protected. Results from these analyses are also used to inform changes to the environmental monitoring programs conducted at each operation.
Corrective action process
We have a corrective action process in place to systematically investigate and address the causes of non-conformance to regulatory requirements or internal standards. The process includes classifying the non-conformance, assigning the appropriate level of investigation (dependent on incident significance), and tracking the recommended corrective actions to prevent and mitigate similar occurrences.
Audits
To support our culture of continuous improvement, our processes and operations undergo regular audits, including:
- Our environmental management system is audited by a third-party every three years as a requirement to maintain our ISO 14001 certification.
- Our SHEQ team conducts an internal audit of our SHEQ programs on a three-year cycle. The total audit scope is split in half and executed on a rotating basis. This means that all our sites undergo at least two audits to cover all aspects of our SHEQ programs within every three-year period. The audit follows the ISO 19001 process and encompasses our environmental and safety programs.
- We also maintain and implement an internal audit program at our corporate office. Results and recommendations from this systematic and documented process are presented to senior management, who are responsible for implementing them and correcting any deficiencies. The internal audit group reports to the audit and finance committee of the board.
Environmental Monitoring
Comprehensive monitoring programs are in place at the McArthur River and Key Lake operations to help ensure that the surrounding environment is protected. Samples of water, air, soil, plants and fish are collected from numerous locations around the sites and tested to confirm that environmental protection systems are effective. Monitoring results are submitted to federal and provincial regulatory authorities for review. Cameco also supports independent regional monitoring downstream of its Saskatchewan operations to ensure there are no cumulative effects on the regional watershed. The extensive monitoring undertaken at McArthur River and Key Lake has identified no significant impact on the surrounding environment.
Environmental Incidents and Other Events
Environmental incidents and other events are reported to regulatory agencies as required by federal and provincial regulations.
Latest incidents or events:
McArthur River
Date | May 10, 2021 |
Incident |
Reportable release |
Details |
An increase in outdoor temperatures caused snow meltwater to accumulate within utilidor sump #7 and approximately 2,000 liters of meltwater overflowed the sump onto the ground. This event is classified as a reportable release. |
Corrective Action |
An alternative pumping system has been set up. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
McArthur River
Date | May 10, 2021 |
Incident |
Reportable release |
Details |
An increase in outdoor temperatures caused snow meltwater to accumulate within utilidor sump #7 and approximately 2,000 liters of meltwater overflowed the sump onto the ground. This event is classified as a reportable release. |
Corrective Action |
An alternative pumping system has been set up. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | March 12, 2021 |
Incident |
Fire alarm system activation |
Details |
The Emergency Response Team (ERT) responded to a fire alarm activation on the third floor east wing of the permanent camp.The Emergency Response Team (ERT) responded to a fire alarm activation on the third floor east wing of the permanent camp. |
Corrective Action |
The ERT team swept the area and determined the fire alarm activation was due to steam. Area was cleared to allow tradespeople to mitigate issue with assistance of ERT team members. Federal regulators were informed. |
Environmental Effect | N/A |
Date | February 8, 2021 |
Incident |
Fire alarm system activation |
Details |
At approximately 12:30 p.m. the fire alarm system in the main camp was activated as a result of light smoke detected in the E-wing. In accordance with emergency procedures, camp residents reported to the designated muster point and the emergency response team (ERT) responded and verified that there was no fire. The cause of the observed smoke was determined to be a damaged belt on the air handling unit. |
Corrective Action |
The camp wing was ventilated and the belt was replaced. Once the area was verified as safe, the alarm system was reset. The CNSC has been notified and follow-up reporting will take place. |
Environmental Effect | N/A |
Date | September 18, 2020 |
Incident |
Fire alarm system activation |
Details |
At approximately 12:30 p.m. a fire alarm was activated underground near the material delivery chute on the 640 level. The emergency response team (ERT) responded in accordance with emergency procedures and verified that there was no fire. |
Corrective Action |
An investigation into the cause of the false alarm is underway. The CNSC has been notified. |
Environmental Effect | N/A |
Date | July 29, 2020 |
Incident |
Fire system activation |
Details |
The emergency response team (ERT), responded to fire system activation in the north-ex refuge station (530 level) underground. The ERT responded in accordance with emergency procedures and verified that there was no fire or smoke. |
Corrective Action |
Investigation indicated that high humidity levels caused a smoke detector to go into alarm. The CNSC was notified. |
Environmental Effect | N/A |
Cameco Environmental Effect Rating
- Level 1 - no measurable impact to the environment
- Level 2 - negligible impact
- Level 3 - short-term, seasonal impact
- Level 4 - mortality of some species, but not affecting ecosystem function
- Level 5 - impairment of ecosystem function
- N/A - not applicable
Key Lake
Date | January 10, 2023 |
Incident |
Radiation Action Level |
Details |
While performing maintenance on a leaching vessel, two workers had an unplanned radiation exposure that led to exceedances of the quarterly action level of 5 mSv. The total annual dose for both workers remains well below regulatory limits. |
Corrective Action |
The workers were removed from the their tasks to complete the follow-up investigation and dose assessment process. The remaining maintenance work on the leaching vessel was completed in accordance with the applicable procedure without incident. |
Environmental Effect | 1 |
Key Lake
Date | January 10, 2023 |
Incident |
Radiation Action Level |
Details |
While performing maintenance on a leaching vessel, two workers had an unplanned radiation exposure that led to exceedances of the quarterly action level of 5 mSv. The total annual dose for both workers remains well below regulatory limits. |
Corrective Action |
The workers were removed from the their tasks to complete the follow-up investigation and dose assessment process. The remaining maintenance work on the leaching vessel was completed in accordance with the applicable procedure without incident. |
Environmental Effect | 1 |
Date | November 25, 2022 |
Incident |
Reportable Discharge |
Details |
Around 3 a.m., technicians were installing a new helium cylinder in the Chemical Lab gas storage room. When removing the plastic safety cover from the new cylinder outlet valve, the helium began venting. The lab gas storage room was immediately evacuated and sealed off to allow the cylinder to safely vent. The discharge of the helium was approximately 30 minutes in duration, which exceeds the reportable discharge duration of less than 10 minutes. |
Corrective Action |
No entry to the gas storage room was allowed until the air monitoring system indicated it was safe. The cylinder was properly secured at the time of the release. It will be sent back to the manufacturer to investigate if the valve was defective. |
Environmental Effect | 2 |
Date | November 24, 2022 |
Incident |
Regulatory Emission Limit Exceedance |
Details |
The Total Suspended Solids (TSS) regulatory emission limit of 30 mg/L for a grab sample collected from treated water was exceeded for a partial pond released at station 1.4, Bulk Neutralization Effluent discharge. Prior to release, analysis of the pond fill sample returned a TSS value that was acceptable for release. During release, the in-line turbidity monitoring interlock system was activated, halting the discharge. Additional samples were taken and returned results that were acceptable for release. Pond release resumed, however, the turbidity interlock system halted the release a second time, and the remainder of the pond was recycled back to Bulk Neutralization for treatment. The pond release sample was analyzed and returned a value of 37 mg/L, exceeding the regulatory emission limit for a grab sample. Approximately 32% (1307 m3) of the pond was released to the environment and 68% (2788 m3) was recycled. |
Corrective Action |
An additional sample was sent to the SRC Analytical Laboratory for further verification. A sample collected on November 25 from the nearest downstream sample location at Station 4.0 Wolf Lake, indicated normal TSS levels. Further investigation is currently underway. |
Environmental Effect | 2 |
Date | October 28, 2022 |
Incident |
Environmental Action Level Exceedance |
Details |
In accordance with site procedures, a pond of treated effluent was released based on the results of the pond fill composite sample. Results for the pond release composite sample indicated the measured value for uranium (81 µg/L) exceeded the action level of 80 µg/l. Measured results for all parameters, including uranium, were well below the applicable regulatory limits. There was no health or safety risk posed to the public, workers or the environment. |
Corrective Action |
Cameco notified the Canadian Nuclear Safety Commission, and an investigation has been initiated. |
Environmental Effect | 2 |
Date | October 22, 2022 |
Incident |
Reportable Release |
Details |
A line at Key Lake’s processing facility released water to the ground. It is believed the line was frozen, causing the release. 6 cubic metres of industrial water was released. |
Corrective Action |
Operations lowered the water level in a tank to prevent further overflow to the line. Environment was contacted to collect samples and Site Services used a vacuum truck to clean up the area. The material was disposed of on site. |
Environmental Effect | 2 |
Date | September 20, 2022 |
Incident |
Reportable Release |
Details |
An estimated 2,000 litres of industrial wastewater from the mine shop pump bay sump were released on the ground when the pump testing pit overfilled with potable water. It was determined that when a hose was placed on the hose rack next to the fill valves, the potable water fill valve was bumped into the “on” position, resulting in the sump to fill and overflow. |
Corrective Action |
The supervisor was notified, and the fill valve was shutoff. The event was reported to the environment and site services departments for investigation and cleanup. Federal and provincial regulators were notified. |
Environmental Effect | 2 |
Date | July 13, 2022 |
Incident |
Event Requiring Reporting to the CNSC Duty Officer |
Details |
The incident command centre has been activated in response to a fire southwest of Key Lake. The Key Lake site is not currently under immediate threat. The Saskatchewan Public Safety Agency (SPSA) crews continue to monitor closely. |
Corrective Action |
The SPSA continues to monitor and provide updates to site. The site re-established a fuel break at the VOR station located approximately 10 km southwest of Key Lake, at the direction of the SPSA. |
Environmental Effect | N/A |
Date | July 5, 2022 |
Incident |
Radiation Action Level Exceedance |
Details |
Elevated monitoring sample measured for worker post CCD thickener maintenance. Preliminary dose estimate indicated a quarterly action level may have been exceeded. Further analysis was required to confirm dose calculations. |
Corrective Action |
All work was stopped in the area until initial investigation was completed. Workers convened for a JHA to discuss procedure for any work in the CCD thickener going forward. Samples were shipped to an external lab for confirmatory analysis. |
Environmental Effect | N/A |
Date | March 29, 2022 |
Incident |
Reportable release |
Details |
At about 10:15 a.m., during daily inspection, ground water from Well V of the Gaertner dewatering system was observed in a small area outside the well shelter. Release volume is estimated at more than 1000 litres. |
Corrective Action |
The reverse osmosis plant feed was re-routed to an alternate well, isolating Well V from the dewatering system. Water samples were collected and site services conducted cleanup. Further investigation into the incident will be conducted after ground thaws. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | February 16, 2022 |
Incident |
Reportable release |
Details |
At about 4:00 a.m., a propane leak was detected near the steam plant. |
Corrective Action |
A faulty propane line was isolated and the area secured. Cause of the line failure is under investigation. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | December 27, 2021 |
Incident |
Reportable release |
Details |
At about 2:50 a.m., an alarm indicated a propane leak on propane pump #2, near the steam plant. |
Corrective Action |
The pump was isolated and the cause of the leak was determined to be a broken pipe fitting to the pressure gauge on the pump. The cause of the breakage is under investigation. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | September 20 and September 27, 2021 |
Incident |
Unusual incidents |
Details |
The weekly effluent sample for the Reverse Osmosis (RO) effluent at Station 1.2 Discharge to Horsefly Lake was not collected on the above dates. Station 1.2.1 Horsefly Lake Outflow was mistakenly collected in place of the Station 1.2 Discharge to Horsefly Lake. |
Corrective Action |
The RO daily product sample results were reviewed, and all parameters analyzed on both days were confirmed to be below the Metal and Diamond Mining Effluent Regulation (MDMER) limits. |
Environmental Effect | 1 |
Date | September 13, 2021 |
Incident |
Reportable release |
Details |
A propane leak was detected in a line outside of the CCD, near the Leaching facility. Corrosion to the piping was observed. |
Corrective Action |
Valve was closed and locked to stop the flow and repairs will be initiated. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | September 7, 2021 |
Incident |
Event Requiring Reporting to the Duty Officer |
Details |
On September 7th, the Emergency Response Team was activated at 10:15am and responded to a non-work-related medical emergency involving a person working at the mill terrace reservoirs. The team was stood down at 10:55am. |
Corrective Action |
The Emergency Response Team responded and provided initial assessment and transported the worker in stable condition to the health centre for additional assessment and care. |
Environmental Effect | N/A |
Date | June 22, 2021 |
Incident |
Reportable release |
Details |
Examination of 2020 and 2021 groundwater sampling results from new monitoring wells indicated elevated levels of parameters such as ammonia and sulfate below the mill terrace area. |
Corrective Action |
An assessment indicates the source is likely a release of water contaminated with barren strip solution. The release is believed to have occurred prior to the operation being placed into care and maintenance in 2018, as tests have indicated there is not an active discharge occurring. Further investigation is underway. Additional drilling and sampling will be completed to further assess groundwater conditions in this area. Inspections and repairs will be completed prior to resumption of production. Provincial and federal regulators were notified. |
Environmental Effect | 2 |
Date | April 18, 2021 |
Incident |
Dangerous occurrence |
Details |
While decommissioning electrical cables in the packaging area, a 120V energized wire was inadvertently cut. This caused the breaker to trip and no injuries occurred. |
Corrective Action |
The electrical wire was repaired and an investigation is underway. Provincial and federal regulators were notified. |
Environmental Effect | N/A |
Date | February 12, 2021 |
Incident |
Reportable release |
Details |
At around 8:15 a.m., a leak detection alarm in Valve Shelter #1 was activated after a damaged 3-inch pipe released approximately 3m3 of water to the floor of the shelter and outside the doorway. Upon investigation, it was determined that freezing temperatures had caused the pipe to split. |
Corrective Action |
A lateral valve in the shelter was closed, which stopped the release. The material was cleaned up utilizing a vacuum truck. The damaged pipe is being repaired. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | October 27, 2020 |
Incident |
Reportable release |
Details |
At approximately 6:15 a.m., workers noted that a water supply line valve in the wash bay had been left open overnight resulting in the release of approximately 12,000 litres of water onto the frozen ground outside the building. |
Corrective Action |
Workers shut off the water supply valve. Water samples were collected for analysis and the slush/ice build-up on the frozen ground was removed for transfer to the Phase IV Ore Pad. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | March 17, 2020 |
Incident |
Reportable release |
Details |
At approximately 2:30 p.m. in the reverse osmosis (RO) facility, the automated shutdown of water pumps failed resulting in the release of approximately 3,000 litres of dewatering water to the ground. |
Corrective Action |
All wells providing water to the RO plant were shut down. Released water, which froze in place on the ground, was removed and placed on the Gaertner special waste pad. Preliminary investigation indicates a system communication power loss, from a UPS failure during maintenance testing, resulted in loss of signal between the high water level alarm and automated pump shutdown system. Provincial and federal regulators were notified. |
Environmental Effect | 1 |
Date | March 8, 2020 |
Incident |
Emergency response team (ERT) activation |
Details |
At 12:24 p.m., the emergency response team (ERT) responded to a burst fire system water line in the stairwell of the mine shop. |
Corrective Action |
Water was isolated and the line was repaired. ERT investigation revealed the line had frozen and burst due to cold weather and heating failure. Federal regulators were notified. |
Environmental Effect | N/A |
Cameco Environmental Effect Rating
- Level 1 - no measurable impact to the environment
- Level 2 - negligible impact
- Level 3 - short-term, seasonal impact
- Level 4 - mortality of some species, but not affecting ecosystem function
- Level 5 - impairment of ecosystem function
- N/A - not applicable
Decommissioning
Detailed plans and financial guarantees are in place to provide for decommissioning of the McArthur River and Key Lake sites when operations end. Decommissioning will include removal of all buildings and equipment and landscaping and re-vegetation of disturbed areas. All underground workings and other mine and mill facilities will be sealed off and secured. A monitoring program will be in place to ensure the sites remain in a secure and stable state for the long-term.
For more information, see:
Preliminary Decommissioning Plan - Summary - McArthur River Operation
Preliminary Decomissioning Plan - Summary - Key Lake Operation
Environmental Risk Assessment
All new, or substantially changed, mining developments may be subject to environmental risk assessments (ERAs) to identify potential effects on the environment. ERAs follow guidance provided by CSA and various agencies, such as Health Canada (HC), Environment and Climate Change Canada (ECCC), Canadian Council of Ministers of the Environment (CCME) and the Canadian Nuclear Safety Commission (CNSC).
In 2020, Cameco completed a detailed quantitative environmental risk assessments (ERA) for its McArthur River and Key Lake Operations to align with the standardized requirements found in CSA N288.6-12 Environmental risk assessment at Class I nuclear facilities and uranium mines and mills (CSA 2012).
Public Summary - Environmental Risk Assessment - McArthur River Operation (PDF 6.7 MB)
Public Summary - Environmental Risk Assessment - Key Lake Operation (PDF 3.8 MB)
Tailings Management
Tailings, or what remains of the ore after the uranium has been removed at the Key Lake mill, is placed in the Deilmann tailings management facility. Commissioned in 1996, the facility is built into the mined out Deilmann pit and is designed to safely contain the tailings during continuing operations and after decommissioning. Tailings are placed in the pit under a water cover. During operations, groundwater is collected from a series of wells around the facility and is treated prior to release to the environment. When operations cease, the tailings will become a solid dense mass and groundwater will flow around the tailings, rather than through them, to minimize environmental impact.
Prior to 1996, tailings from the Key Lake mill were deposited in a surface tailings management facility approximately 600 metres by 600 metres and 15 metres deep. The facility was constructed five metres above the groundwater table and used a modified bentonite liner to isolate the tailings from the surrounding soil.
Regulatory Oversight
The primary regulator for the McArthur River and Key Lake operations is the Canadian Nuclear Safety Commission (CNSC). These operations are also subject to regulatory oversight from several other federal and provincial agencies including Saskatchewan Ministry of Environment. Federal and provincial regulators conduct regular site inspections and audits to verify that people and the environment are protected. Uranium mining and milling operations in Canada are licensed by the CNSC.
Sustainability at Cameco
When measuring the sustainability and ethical impact of a company, environmental, social and governance (ESG) are key factors considered by the public and investors. Sustainability and ESG matters have been an important focus at Cameco for many years and we have a strong performance record.